






I set-up on the far North end in a patch of shallow weeds. There was a nice down hill grade and even if I had to Taxi into some tall stuff, I figured that I would be moving fast enough to plow right through. Marek got off first and I was right behind him. We both went north past the dam and I chased him west into the sun.
When I was at the West end of the lake I cut the corner and approached Marek from behind getting several good shots and i caught and passed him. Then we headed over to the High Schoola and Marek played low while I played high. I did a tight spiral dive and flew through my wake. WOW! The Thumper has a much bigger footprint than the Simonini had. Marek flew through it as well and he claims that the WACK bounced him 3 inches above his seat.
When I realized that my life was being supported by a glorified key
chain and some thin 1/2 inch webbing...
I thanked the Creator that I was still alive.
Then I looked for the best way,
to proceed to earth…
as directly as possible.
I'm still shaking my head trying to figure out how it happened.I attached the riser on the left side to the cheap plastic beaner that I use for the foot steering instead of connecting to the heavy stainless beaner that ties the wing to the buggy. I didn't realize my mistake until I noticed that the foot steering cable was pressing against my left side. When I saw that the rig was being supported by a glorified key chain and thin 1/2 inch webbing...I couldn't believe that I was still alive. Not only was the beaner unrated and not designed to carry a load, the loop it was attached to was loaded against the stitching. There were two places where a failure was imminent. Looking at the materials it should have failed when I loaded the wing before take-off ...and... I wish it had. It would have been more dramatic and made a bigger impression but it wouldn't have killed me. As it was a non-incident, I hope that the magnitude of the error sticks with me.
I had to get down ...right now! I was 400 feet AGL and about the correct distance to glide back to the field, so I did a slow flat turn toward the field and landed without incident.
What were the causes that lead to this huge goof ?
1. I had switched to the Eden III which does not require the extra loop of webbing to get the hangpoint right. When it is configured this way the hangpoint loops are not long enough to reach the normal keeper on the bullet bars. So...I end up attaching the beaner to a loop on the foot steering for transport.
2. I must not have had enough coffee because it is almost impossible to imagine an alert mind attaching a plastic carabiner to the riser. It is so much more difficult to thread the correct carabiner that it should have set off alarms when that slim plastic beaner tip slipped through the loop so easily. The length was about right and when I pulled on the riser to take out any slack, it pulled the hangpoint loop just as if it were correctly attached.
I thought perhaps I should move the foot steering forward on the bullet bars to get them away from the hang point straps, but I don't think I'll do that. Having the webbing behind my shoulders is cleaner and I doubt I'll ever look at the foot steering again without remembering the day I hung from a cheap 2 inch plastic carabiner.
This is the first real stupid mistake I've made in PPG and certainly the first one that endangered my life! I was deeply affected by the experience, and it was heavy on my mind for several days. I will strive to learn from this and be a more responsible pilot.
I vote for better pilot.

When I got back to the field the wind had shifted to South West and bumpy. At 100 feet the wing started to oscillate but it corrected in time for a safe 3 point landing.
Early bird gets the glass


I had to use the small American Flags for wind socks because I had forgotten my big one. Not to easy to spot when I'm trying to land but they worked well as long as I was sitting.
I would have loved to take some pictures but it was active flying and I didn't feel comfortable going no hands.